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电动汽车用A123电池起火事件调查报告

电动汽车用A123电池起火事件调查报告
电动汽车用A123电池起火事件调查报告

REPORT OF INVESTIGATION: HYBRIDS PLUS PLUG IN HYBRID ELECTRIC VEHICLE

Prepared for:

National Rural Electric Cooperative Association, Inc.

And

U.S. Department of Energy, Idaho National Laboratory

By:

Garrett P. Beauregard

V.P. of Engineering

Phoenix, AZ

June 26, 2008

Revision 1

Acknowledgement

ETEC wishes to thank the following organizations for their support, expertise and participation in this investigation:

?Hybrids Plus

?A123 Systems

?NRECA

Introduction

ETEC was recently retained by the National Rural Electrical Cooperative Association (NRECA) and the U.S. Department of Energy, Idaho National Laboratory to lead an investigation of a fire in a Toyota Prius that had been converted to a Plug-In Hybrid Electric Vehicle (PHEV) by Hybrids Plus. This document presents the report of that investigation and the determination of the root cause of the fire.

Background

In February, 2008, the Central Electric Power Cooperative, Inc. (CEPCI, Colombia, SC) purchased a Toyota Prius and had it converted to a PHEV by Hybrids Plus (Boulder, CO). This vehicle was designed to be a PHEV-15 meaning that it had a battery pack sized to provide 15 miles of all-electric driving. To effect this conversion, Hybrids Plus replaced the stock Toyota battery pack and replaced it with a higher-capacity pack fabricated using lithium-ion cells purchased from A123 Systems (Watertown, MA).

On Saturday, June 7, 2008 a CEPCI engineer was driving the PHEV Prius. The reported high temperature that day was 98F. After approximately 40 miles of highway driving, The driver noticed a warning light on the Prius’s display screen and simultaneously noticed that the combustion engine was operating at high rpm. He pulled the vehicle to the shoulder, turned the car off and inspected the vehicle. At that time, he noticed an acrid smell but attributed that to the high rpm operation of the engine. The driver restarted the vehicle and pulled back onto the highway, accelerating quickly to achieve highway speed. After another four-to-five miles, the driver again experienced a warning light on the vehicle display (although the engine did not operate at high rpm this time) and noticed a strong odor of burning material. He opened the windows and began to pull over. When the windows were opened, a significant amount of smoke was pulled forward to the driver’s area. The driver exited the vehicle and noted a fire at the right side in the rear (cargo) compartment of the vehicle which eventually consumed the vehicle. Figure 1 shows the results of the fire (See Appendix A for additional images of the fire-damaged vehicle).

Figure 1--Fire Damaged PHEV Prius

The vehicle was towed to Firmin Ford (Laurens, SC), a close, convenient spot for the tow truck driver. Davide Andrea of Hybrids Plus was dispatched to Columbia where he performed the initial inspection of the vehicle. During this inspection, Mr. Andrea found that there was still voltage present at the battery pack, although not as high as would normally be present on this pack. Mr. Andrea cut several cables on the pack to reduce the available voltage in an effort to make it safer to handle. After completing his initial inspection, Mike Hoff and Ricardo Bazzarella of A123 Systems arrived in South Carolina to inspect the vehicle. Following that, a determination was made by Hybrids Plus, CEPCI and A123 to remove the battery pack and transport it to A123 Systems’ facility in Hopkinton, MA for further investigation. Ricardo Bazzarella of A123 Systems transported the battery pack in his rented vehicle back to Hopkinton.

Design

ETEC’s VP of Engineering, Garrett Beauregard, traveled to Hopkinton on June 13 to participate in the battery investigation. A team was assembled consisting of several engineers from A123 Systems, Carl Lawrence, CEO of Hybrids Plus along with ETEC’s Mr. Beauregard. The chain of events leading to the fire was first reviewed. Following that, the Hybrids Plus battery design was reviewed.

The Hybrids-Plus battery pack is based on the A123 Systems Lithium-Ion cell which uses a Nanophosphate1 technology to limit the reactivity of these cells. The cell uses an aluminum can which contains a roll of copper and aluminum foil onto which the active materials are coated. A flammable, solvent-based electrolyte is used. The cell is sealed with a laser-welded cap which is machined with a relief groove that turns this cap into a rupture disk should internal pressure build beyond a design point (the pressure vent). A fill hole is present on the anode end of the cell through which the electrolyte is loaded into the cell. This hole is sealed with epoxy. As the sides of the cell can are at anode potential, the cell is placed inside a heavy, cardboard sleeve (rated UL 94 V-0, self

1 A trademark of A123 Systems

extinguishing). With the sleeve in place, only the ends of the can are available to conduct energy. Figure 2 shows the features of the A123 cell.

Figure 2--A123 Lithium Ion Cell

The battery pack consists of 600 cells arranged in a 10P 60S configuration; groups of 10 cells connected in parallel joined into a series string of 60 of these groups.

The parallel groups are created by spot welding the poles (all positive or negative) of the cells to a Nickel sheet which acts as the bus bar. Each A123 cell has a Nickel disk (or rivet depending on which pole) attached at the end of the can to facilitate welding to the Nickel bus bar. See Figure 3 for details.

Figure 3--Bus Bar Arrangement

The 600 cells are arranged in four large “batteries” which consist of 160 cells (front batteries, 16 series strings of parallel groupings) or 140 cells (rear batteries, 14 series strings of parallel groupings). These four batteries are created by welding the cells to Nickel sheets (used as bus bars) and then enclosing this construction into a plastic

clamshell housing which is vacuum formed from Boltaron 1165 (Acryllic/PVC alloy plastic). The two halves of the clamshell are adhesively bonded together. Figure 4 is a typical battery assembly, although not identical to the one used in the PHEV 15 Prius. Figure 4--Assembled battery

The four batteries are stacked two high and two deep so that the following descriptions are used:

?Bottom Front2

?Top Front

?Bottom Rear

?Top Rear

Figure 5 shows a close up of the left-hand end of the four-battery assembly.

2 Throughout this document, typical automotive convention is used—front is vehicle front and right is driver’s right when seated in the driver’s seat and facing the steering wheel

Figure 5--Four-Battery Assembly

The four batteries are restrained by the top cover which is bolted to the vehicle’s chassis in the original battery mounting locations; there is no mechanism for restraining the individual battery assemblies. Figure 6 shows the battery pack with the cover in place.

Figure 6--Battery Pack Assembly with Cover

Figure 7 presents a general schematic for electrical connection of the batteries as they are configured in this pack.

Bottom Rear Battery

Top Front

Battery

Figure 7--Hybrids Plus PHEV 15 Battery Schematic

Although not shown on this diagram, each battery is equipped with a 250A fuse that is connected directly to the Nickel sheet grouping one parallel set of 10 cells via a tab that is formed in the Nickel sheet. A brass nut is soldered to the back of the tab and a brass bolt is run through the blade at one end of the fuse and into the brass nut on the back of the tab (therefore, the fuse blade and Nickel tab are clamped together. The other fuse blade has a brass nut soldered to its back side. The fuse is encased in the plastic clamshell. A small square of open-cell foam is located between the fuse and the cells which is used to push the fuse blade out toward the plastic cover so that the bolt will more easily engage in the threads of the nut on the back of the blade. This foam is known to be flammable from tests conducted at Hybrids Plus and at A123 Systems. A hole is cut in the clamshell so that a lug can be attached to the fuse via another brass bolt. The opposite end of each battery (physically and electrically) uses a brass nut soldered onto the back of the formed tab with a hole cut into the clamshell to allow for the attachment of a lug. See Figures 8 and 9.

Figure 8--Formed Tab Figure 9--Battery Terminal

Each parallel group is monitored for voltage and temperature by small printed circuit boards soldered to tabs on the Nickel sheets at the top and bottom of each group. The temperature sensor is a component on the circuit board and is not in contact with any of the cells; it is instead located in the interstitial space between two adjacent cells. Battery Inspection

The battery was wrapped in plastic sheet and located on a table in A123 Systems’ assembly area. The plan of action was to slowly and methodically inspect, document and remove components from the battery pack to look for the initiating point. Upon initial viewing, it was apparent that the right end of the battery pack was most severely damaged in the cavity that is formed between the front and rear batteries (the batteries are designed so that a U-shaped pocket is formed on the right end to provide clearance for cables that attach from front to rear batteries). Much of the clamshell was missing or severely melted in this area. Several cells from both the Front and Rear top batteries were found open with their contents missing or protruding from the can. See Figure 10.

Figure 10--Empty Battery Cells

In the middle of Figure 10, a heavy cable can be seen with the remnants of a fuse connected to it. This is the Cross Connect Cable that connects the Front Bottom battery to the Rear Top battery. The plastic housing of the fuse is missing (melted or baked away) but the fuse is still intact. In fact, all of the three intact battery fuses were still electrically conductive. The main pack fuse (125A) was also electrically conductive. The cable connecting the Rear Bottom battery to the Front Top battery was not attached to the assembly but was present (loose) with the battery. This assembly had the fuse from the Rear Bottom battery still attached and a portion of the Front Top fuse attached (Figure 11).

Figure 11--Interconnect Cable

Again, the intact fuse had a severely melted housing but the fuse was still electrically conductive. A microscope examination of the partial fuse shows that the fuse suffered a mechanical break and likely did not melt in an overcurrent condition (Figure 12). Examination of photos taken of the vehicle shortly after the fire show that this fuse was intact after the vehicle was towed to Firmin Ford. The fuse was likely broken during the vehicle investigation in South Carolina.

Figure 12--Broken Fuse

On checking the left-hand end of the battery pack, it was noted that the burning and melting of components wasn’t as significant as that found on the right-hand end.

After thoroughly inspecting the assembly, the pack was disassembled so that all four batteries were removed from the steel tray. These were marked to note their location. In order to examine the individual cells and any damage that was present inside the batteries, the Top Front battery was cut apart and removed (Figure 13—the remaining three batteries were shipped to Hybrids Plus for their inspection).

Figure 13--Opening the Clamshell

With the batteries removed from the tray, the terminals on the left-hand end (non-fused) could be more closely examined. On all four batteries, these connections were found to be loose (Figure 14).

Figure 14--Non-fused Terminal

With the clamshell removed, all cells inside that battery could be visualized. It was noted that significant burning was present at the right-hand end, some heat deformation of the plastic and soot on the cells at the left-hand end and little damage in the middle except at the front face where a significant amount of melting occurred (Figure 15).

Figure 15--Burn Pattern in a Battery

The cells were removed from the clamshell housings to allow for inspection of the cells and Nickel sheets on the bottom side. Nothing unusual (beyond the same burning seen from the top) was noted.

Following the cell inspection, the lugs/fuse/bus bar interfaces were examined. During the design review, it was noted that the clamshell design creates a situation where the plastic clamshell is placed between the fuse blade and the interconnecting cable terminal. Mr. Lawrence of Hybrids Plus indicated that the design required that a bushing or spacer be placed between the fuse blade and the terminal so that the plastic would not be placed in compression. Upon inspection of the various connections no spacers were found between the terminal and the fuse (or the bus bar tab in the case of the non-fused locations. See Figure 16 for some examples and Appendix C for an assembly diagram.

Figure 16--Terminations

While examining the various terminations, several of the fused connections were found to be loose (Figure 17).

Figure 17--Loose Terminations

During this inspection, it was also noted that there was significant transfer of material between the brass bolts and nuts, the cable terminals and the fuse blades (Figure 18). This material transfer is indicative of significant electric arcing and very high temperatures. Figure 18--Material Transfer at Terminations

The Nickel sheet bus bars were also closely examined. The great majority of spot welds appeared to be intact. Where cells ejected their contents, some spot welds were torn where the Nickel sheet was lifted up and away from those cells. In some cases, the spot welds were intact and the Nickel disks used at the ends of the cells were still attached to the sheet Nickel. It was also noted that the tabs on the Nickel sheets formed to be the attachment location for the fuses were all missing. They were found still attached to the fuse blades. All of these remnants exhibited signs of melting at their edges as opposed to stretch or fracture marks. See Figure 19.

Figure 19--Torn Tabs

During this inspection, two curiosities were noticed with regard to the Nickel bus bar sheets. The first was at the Top Rear battery on the right-hand side. The Nickel sheet was no longer attached to a cell. Instead, the Nickel sheet had a circular hole in it and the missing portion of the sheet was still attached to the top of that cell (Figure 20). The area around the circular hole show signs characteristic of excessive heating.

Figure 20--Circular Feature3

The second feature was located at the Top Front battery on the right-hand side. A cell at the corner of the second series group and located at the corner of a Nickel sheet had become disconnected from the rest of its group, taking the corner of the Nickel sheet with it (Figure 21). The crescent-shaped area on the remaining Nickel sheet shows characteristic signs of excessive heating.

3 Some debris and charring was removed from the Nickel sheet using a plastic-bristle brush to more clearly

see the features on the sheet.

Figure 21--Torn Corner Cell

See Appendix B for a collection of images recorded during the inspection. Determination

The inspection of the battery led to the conclusion that the fire was most likely the result of a loose connection, probably at the right-hand side of the Bottom Rear battery. This connection was found to have a nearly 0.1” gap between the bolt head and the lug (Figure 22).

Figure 22--Loose Connection

As can be seen in the photo, this assembled joint was found with the bolt screwed only partially into the nut. It is unlikely that this occurred during either of the vehicle or battery inspections as it required wrenches to remove the nut from the bolt. More likely, this was a result of a) the lack of a locking device to prevent the bolt from backing out, b) the lack of a spacer between the fuse blade and the lug which placed the plastic of the clamshell housing in compression between the two and c) vibration from normal vehicle operation causing the bolt to back off from its original installed position. This joint was found to have approximately 0.16” clearance in the assembly. Assuming that the

clamshell plastic was nominally 0.06” thick, the clearance at the time of the fire would be approximately 0.1”.

As a current-carrying joint becomes loose, the resistance of the connection increases. The power dissipated in heat by a resistor is given by P=I2R. Therefore, a doubling of the resistance increases the power dissipated by heat by a factor of two. The battery pack will experience a maximum discharge current somewhere near 100A during normal driving. Given that the power dissipated by heat is proportional to the square of this current, an increase in resistance to even a few Ohms will result in extreme heat generation. Experience shows that loose connections can lead to temperatures over 250°F.

Once the lug began to heat, that heat was transferred up the copper Cross Connect Cable as copper is an excellent conductor of heat. This heat passed through the connection to the Top Front battery fuse, through the fuse and into the cells through the Nickel bus bar sheet. This heat would also cause the plastic clamshell housing to soften in that area. The soft plastic would be unable to withstand the clamping load and would displace where the lug mounted to the fuse (sandwiching the plastic). This displacement likely resulted in the connection at the Top Front battery (fuse end) to become loose, adding to the resistance in the circuit.

The initial theory was that this heating caused the insulation to fail on the large-gauge Cross Connect Cables that connect the four batteries at the right-hand end of the pack. At this location, two cables were installed—one that connected from the Bottom Rear battery to the Top Front and one that connected the Bottom Front battery to the Top Rear. The assumption was that the insulation failed and caused the bare copper to touch and short. However, assuming that both cables had loose connections and the insulation burned, melted or otherwise failed, the short-circuit current would have been significantly higher than the 250A fuse attached to each battery, causing at least one fuse to open. All four fuses were found intact (the fuse at the Top Front battery was broken at some point after the initial vehicle inspection but before it reached A123 System’s facility). Instead, it is more likely that heat continued to build up in the system through the loose connection and that this heat was conducted into the cells of the Top Front battery. Once this battery built up sufficient internal heat, it began to develop gas pressure internally and eventually ruptured the cell at the designed pressure vent point.

It should be noted that there was likely an additional source of heat generation. Due to the placement of the connecting tab at the edge of the Nickel sheet and the layout of the 10 cells in each parallel group, the cell closest to the tab would experience a higher current throughput than the rest of its parallel group mates. This additional current would tend to make this cell run warmer than the rest. Therefore, the cell in the Top Front battery where the tab was located would have been running warm to start with, and would be the first to receive heat conducted via the Cross Connect Cable, through the fuse and into the tab. The temperature sensors used to monitor the temperature across the parallel groups in a battery were likely very slow to respond to this internal cell heat. The fact that they were not in contact with any cell and that each cell is somewhat thermally insulated via the cardboard sleeve means that heat conduction into the temperature sensor would be a slow process, lagging greatly behind the actual temperature of the cells.

The design for the Nickel bus bar sheeting served to restrain the cells so that it is likely that the actual pressure required to rupture the vent would be much higher than its design rating. That is, if we assume that the pressure vent is designed to rupture at 100 psi (an

arbitrary number for the purposes of this example) and the pressure vent is 1” in diameter, the resulting force required to rupture the can is 100*.52*PI = 79 lb. However, the Nickel sheet would begin to stretch as the pressure vent began to deform in the rupture process. This stress would apply a force in the opposite direction of the force being applied from the inside of the cell. Thus, a higher pressure is required inside the cell to generate enough force (or delta-force) to overcome the opposing forces imparted by the stress in the Nickel sheet in order to rupture the pressure vent.

Once the cell built up enough pressure, the pressure vent ruptured and the contents of the cell were ejected with great force; enough to rip the tab off the end of the sheet (the fuse was captured inside the clamshell next to the cells), to pull the Nickel sheet off several adjacent cells and to punch through the plastic clamshell cover (likely softened due to the heat). See Figure 23.

Figure 23--First Rupture Site

It is likely that the tab on the Nickel sheet was ripped off first as there is evidence of melting, a sign that current was passing through this area which resulted in arcing as the tab became separated from the sheet.

With the first cell ruptured, an amount of electrolyte would have spilled out of the cell can. Any arcs or sparks in the area would have caused the electrolyte to burn which in turn would cause the foam behind the fuse to burn.

When the first cell ruptured, pieces of the foil roll may have become separated from the roll and come in contact with the next adjacent cell. This cell is part of the next series group of 10 in parallel. As such, contact between these two cells would have caused a short circuit between these two series groups and all the current would have flowed

through these two cells. This is the likely cause of the cell at the corner where the Nickel sheet is separated. Such high current would have caused the Nickel sheet to melt (1560°C), acting as a fuse for the rest of the parallel group.

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